(Image/Jeff Smith)

It all began with a cast-off 283 small-block Chevy. The ’64 El Camino limped into our garage spitting out of the carburetor and suffering from severe palpitations. By all indications, it was near death. We pulled the engine and banished into a back corner where it oozed dark stains for years. With shop space at a premium, it was time to decide whether to revitalize this wheezer or truck it off as smelter fodder.

We chose to give this small block new life.

The 283 was Chevy’s base V8 during the 1960s. Nearly every Chevrolet model built during that turbulent decade employed this journeyman small-block. Today, while not extinct, it has become a bit of a novelty, notable if for no other reason than it simply will not go away. We decided to save this one mainly because it seemed worthy of the effort—like finding an old dog in the city pound who’s counting on your compassion to save his life.

Digging into the Engine

The 283’s symptoms were the clues to its problem. The popping from the intake was the result of a flat exhaust lobe. A friend once warned us “Don’t start small projects!” We should have listened. This restoration began as a simple cam swap but quickly evolved into much more. The plan was to quickly disassemble this small-block, clean it up without removing the pistons or crank, install a new cam and intake manifold and then put it to work as a daily parts chaser in a ’53 Chevy pickup that we don’t own—yet.

With the oil pan and front cover removed, the cam revealed three lobes approaching oneness with a perfect circle. The surprise came when we noticed a mismatched pair of 76cc chamber heads. We knew from playing with compression ratio programs (like the one on Summit Racing’s website) that large volume chambers absolutely kill compression on short-stroke engines like this 283. As evidenced in the Compression Lessons footnote near the bottom of this story, these heads combined with thick 0.050-inch composition head gaskets, sink the ratio down to a weak 7.4:1.

The next surprise was when we discovered the bore was 4.00 inches! Research revealed this as an original 1964 283 block, someone had punched it from 3.875 to an even 4.00-inches. This put the displacement at 301.6 cubic inches. This is similar to what Chevy did in 1967 to create the ’67-’69 302 Z28 engine, except that the factory employed a 4.00-inch bore 327 small-journal block to pair with the 3.00-inch stroke 283 crank. Before 302 became the new buzzword, ‘60s hot rodders called this combo a 301. What encouraged us was the lack of a wear ridge at the top of the piston travel.

We performed a leak-down test before we snatched the heads and found, not too surprisingly, that it leaked between 30 and 40 percent. We think this number is actually high by 10 percent since we could hold the crank in place with a breaker bar just past top dead center (TDC) and the percentage improved by 10 percent or more. All the leakage appeared to be coming past the rings. We thought about pulling the pistons to install new rings but we avoided that temptation.

We then searched and uncovered an abused pair of original 283 heads with 3795896 casting numbers. These were used on Power Pack 283 and even 250 hp 327 Corvette engines in 1964. These heads employ a 60cc combustion chamber along with diminutive 1.72/1.50-inch valves. The heads had been rebuilt at least once and featured decent bronze guides but then were criminalized with those terrible white, hard plastic valve guide seals. We pulled the heads apart and threw those PC seals in the trash. 

The 283 Rebuild Begins

We delivered the heads to Barrington Machine in Canyon Country, California where Don, Jr. performed a complete cleaning and Magnaflux check for cracks. With a clean bill of health, he installed hardened exhaust seats, added a 3-angle valve job, and milled the deck surface flat, which removed about 2cc from the chambers. This required an investment of around $700, but we knew putting money into cylinder heads like these (even with small valves) will always be rewarded with better performance.

We chose the less expensive route of rebuilding a stock set of heads, but this comes at the cost of reduced airflow. If more power is something you’d like to achieve with a similar small displacement engine, there are now several head offerings that are worth investigating. A stock bore 283 (3.875-inches) or 305 (3.736-inhces) cannot accommodate 2.02-inch intake valves because the valve will hit the small bore. To satisfy this market, Edelbrock, World Products, Trick Flow and others now offer heads with smaller 1.94/1.50-inch valves with 60cc chamber heads that will do the job. The least expensive of these are the World Products iron heads that will command about twice the price of what we spent to rebuild our stock heads. Any of these small-valve, small chamber heads would be a great choice to upgrade one of these early engines.

With the heads out for refurbishing, we poked around on Summit Racing’s website and found an extremely affordable flat tappet hydraulic cam. Our goal was a smooth performing engine that would exhibit excellent street manners yet still make a little more horsepower than stock. The higher horsepower 283 engines from the early ‘60s were rated between 220 and 230 hp. As you can see in our cam spec chart near the bottom of this article, the Summit Racing cam is very conservative with only 204 / 214 degrees of duration for the intake and exhaust respectively.  Small engines like this overgrown 283 will just lose torque with a bigger cam while not adding the equivalent peak horsepower because of the small heads. With large-valve aftermarket heads, this is a different story but, for our setup, we felt this combination would deliver an excellent all-around package.

As for the intake, Summit Racing has several levels of dual plane intakes but we chose the smallest again to match our diminutive displacement. This was part of a Summit Racing Pro Pack combo package that includes gaskets, RTV, a chrome air cleaner, and a 600 cfm Summit Racing four barrel carburetor. We’ve had great prior experience with this carburetor and its annular discharge primary boosters. Combine this small carburetor with a dual plane intake, small intake ports with good velocity, and good compression, and our 301 promises to be a nice combination. Now all we had to do was assemble the package.

Putting it Together

The first step after we had cleaned the short block was to install the cam. We used a moly-based cam coating on all the lobes and also on the bottom of the Melling lifters. We also made sure there were no sharp edges on the lifter bores that might cause problems. With the cam and a new timing set in place, we also took the time to degree the cam using the centerline method. With that set, we then glued down the oil pan gasket and installed the timing cover and oil pan.

By this time, Barrington had completed the machining on our heads and they were ready to be bolted back in place. Because the pistons were so deep in the hole, we chose a Fel-Pro 0.015-inch head gasket that would help bring the cylinder head closer to the tops of the piston. This improves what is called the quench area as well as increasing compression. As you can see from our Compression Lessons footnote, our efforts were rewarded with a 9.43:1 squeeze factor. That’s a full 2 numbers greater than what it had before.

If we were building a high-end small-block where all the details needed to be exactly right, we’d definitely go with pistons and rods that would bring the tops of the pistons much closer to the deck surface and likely deck the block. But that money wasn’t in the budget, so we’ll just have to live with the 0.030-inch piston-to-deck clearance. We checked another 283 not long ago and found that it too suffered this same malady.

We also caught a small item that might have caused some tuning problems later. The original harmonic balancer had seen better days, so we ordered a small diameter 6 1/8-inch, Dorman balancer and performed a quick check to ensure TDC. That’s when we discovered that even though this balancer is intended for early small-block Chevys, the woodruff key has been machined for a 1969 and later small-block.

The difference is significant. If we used the original 283’s welded-on timing tab, the timing was 12 degrees retarded. In other words, had we used the original timing tab, 12 degrees advanced on a timing light would actually be 0 degrees! We just bolted a late model timing tab over the stock tab and now the TDC mark is accurate. It’s the little things that can make a big difference!

Surprisingly, the valve springs on the old heads were in really good shape giving us 105 pounds on the seat with an installed height of 1.770-inches and 200 pounds of open load at 0.500-inch lift. These numbers are on the low side for a high rpm small-block, but for our mild little street motor this will put less load on the new cam during break-in. We also re-used the original stamped rockers and pushrods since they were in good shape. If you are using new stamped rockers, make sure all the rocker balls are coated with quality high-pressure lube like molybdenum sulfide. Sometimes an exhaust rocker may gall—so watch for that after break-in. If one does gall, the rocker body will turn blue or black.

With the rockers in place we still had to set preload since this is a hydraulic lifter camshaft. We won’t run through the details but it’s a simple process. If you need help with this, you can refer to a story we’ve written for the Summit Racing Basics Series here. Our process is very simple and only requires that you remember the initial EO-IC, which stands for exhaust opening and intake closing. When the exhaust valve is opening, you set the preload on the intake side. When the intake is closing, you set the preload on the exhaust side for that pair of rockers on that cylinder. If you are unsure of this process, our story should make it clear.

Priming and Final Prep

After bolting on the intake with our Fel-Pro gasket set, we filled the oil pan with Summit’s Break-In 30 viscosity oil and used a Summit pressure lube tool to spin the oil pump with a ½-inch drill motor. We removed both valve covers so we could see when all 16 pushrods had oil spilling into the rocker arms. This can take a few minutes so be patient. It’s important that the entire engine is pre-lubed. It’s also worth noting that you should use the proper pre-lube tool. If the channel in the body of the pre-oiler is not used, oil will not reach the right side oil gallery and the lifters will not receive any oil. Look at a typical small- or big-block distributor and you can see where the channel exists near the bottom of the distributor just above the drive gear. This is why a simple shaft will not suffice to direct oil to the entire engine. On a small-block Ford, a simple shaft will work as there is no requirement for a cross-over channel.

With the pre-oiling completed, we like to set the crankshaft at 12 degrees Before Top Dead Center (BTDC) with the Number One cylinder building pressure. You can tell this by holding your finger over the Number One spark plug hole. When pressure starts to build, this is compression stroke and then you can set the timing tag at 12 degrees. Then it’s an easy matter to drop the distributor in and set it to point directly at the Number One position on the distributor cap. These steps are critical to ensuring the distributor is installed correctly. If you’re not sure how to perform all these steps, we’ve written a complete step-by-step article on how to install a distributor and set timing here. With the distributor in place, we hooked up a set of spark plug wires and a new set of Autolite spark plugs, and our engine was ready to fire.

Engine Break-In

With our engine bolted to the test stand, we had 12 volts to the HEI distributor and primed fuel from the carburetor and the engine started literally on the second crank. With the engine running, we immediately brought rpm up to 1,500 rpm and varied the engine speed by slowly moving the throttle between 1,500 and 2,000 rpm. This higher engine speed ensures plenty of splash lubrication on the camshaft. This is how the lifters are lubricated which is why the additional engine speed is important.

We kept an eye on the oil pressure and water temperature. At first we were a little concerned because the right side exhaust belched some oil for about 20 seconds of running time but then that quickly cleared up.

With the full cooling system on our test stand, the coolant temperature never exceeded 185 degrees. If engine temp exceeds 210 degrees F, slow the speed down to idle and quickly shut it down and allow the engine to cool. The entire break-in process should take between 15 and 20 minutes. If you desire, after 10 minutes of initial run-in the engine can be driven—as long as it is not allowed to idle for more than a few seconds before the 20 minutes of break-in is complete.

We had a small oil leak around the front oil pan seal to the timing cover that required some attention, but otherwise the engine ran smoothly all during the break-in process. After break-in we checked the initial timing at 12 degrees and the mechanical advance added another 22 degrees for a total of 34 degrees of total timing. Then we set the idle mixture on the carburetor to the highest idle vacuum setting and then leaned the adjusters by roughly 1/16-turn for the best lean idle mixture at 850 rpm.

The Results

With the higher compression ratio, the engine sounds snappy and is very responsive to throttle changes. Once we find the suitable donor vehicle, we’ll run the engine in a car for about 100 miles and then change the oil and filter, using five quarts of high-zinc 10w30.

While we had to invest a few more dollars into this engine than we originally intended, we now have a strong, responsive small-block that has been brought back from the brink of destruction and is now ready for miles of care-fee cruising.

Compression Lessons

This chart reveals how important it is to measure the actual components and to compute the true compression ratio. When we disassembled this engine we discovered it had large, 76cc combustion chamber heads, 0.030-inch average piston-to-deck height (less than ideal but typical of ‘60s engines), a 0.050-inch thick head gasket, and pistons with four valve reliefs that add approximately 6cc to the total volume. These measurements combined to produce the ridiculously low compression ratio of 7.27:1 in Combination A. Combo B switches to a 64cc chamber and a 0.015-inch head gasket. Combo C uses a 0.038-inch composition gasket and the smaller 58cc chamber. The final Combo D is the package in our 301 that created the most compression was a 58cc chamber and a 0.015-inch head gasket. Note the amazing change from 7.27:1 to 9.43:1 – this is more than a 2-point increase in compression ratio. That alone is worth roughly 6 to 8 percent power. An 8 percent improvement on a 300hp engine is worth approximately 24 horsepower!

ComboABCD
Compression Ratio7.27:18.79:18.92:19.43:1

Cam Specs for Last Waltz 283

CamshaftAdvertised DurationDuration at
0.050"
LiftLSA
Intake278°204°0.421"112°
Exhaust288°214°0.444"112°

Parts List for Last Waltz 283

ComponentPart #Quantity
Summit Racing Classic CamshaftSUM-11021
Melling Replacement Hydraulic LiftersMEL-JB-81716
Summit Racing Intake Manifold, Carburetor, and Air Cleaner Pro PackCMB-03-01901
Summit Racing Harmonic Balancer Bolt KitSUM-G16771
Summit Racing True Roller Timing SetSUM-G6600R-91
Melling 1.72" Intake ValvesMEL-V03998
Melling 1.50" Exhaust ValvesMEL-V04008
Summit Racing ZDDP Performance Break-In OilSUM-1-SAE305
Summit Racing ZDDP Performance Motor OilSUM-1-10W305
Summit Racing Valve Covers SUM-G33061
Summit Racing Valve Cover GrommetsSUM-G34112
Summit Racing Valve Cover Hold-Down TabsSUM-G34342
Summit Racing Mechanical Fuel PumpSUM-250000-11
Summit Racing Cast Iron Water PumpSUM-3123541
Summit Racing Water Pump PulleySUM-G39591
Summit Racing Crankshaft PulleySUM-G39611
Dorman Harmonic BalancerRNB-594-1561
Summit Racing Extended Life Oil FiltersSUM-1270042
Fram PCV ValveFRM-FV1911
Fel-Pro Performance Head GasketsFEL-10942
Fel-Pro Engine Gasket KitFEL-260-10001
Edelbrock Valve SealsEDL-97251
Summit Racing Blueprinted HEI DistributorSUM-850001R1
Summit Racing Oil Pump PrimerSUM-9010151
Summit Racing 8.5mm Ignition WiresSUM-8890111
Autolite Copper Core Spark PlugsATL-A868

This is where we stashed the 283 leaking oil on the floor. It was saved from scrap heap destruction, but just barely. (Image/Jeff Smith)
Before we yanked the heads, we performed a leak-down test. Most cylinders averaged 40 percent but we think once it’s all buttoned back up that this will improve–especially after the engine has run and warmed up. (Image/Jeff Smith)
With the heads removed, there was a hideous layer of carbon on both the piston tops and the combustion chambers. After cleaning a piston to check deck height, we discovered Number One piston was 0.030-inch below the deck height. Worse yet, the previous owner used a 0.050-inch head gasket which put the piston 0.080-inch from the head and killed the compression ratio. (Image/Jeff Smith)
We found two lobes that were nearly round with heavily worn lifters – time for a new cam and lifters. (Image/Jeff Smith)
Note the horrific clump of carbon on the exhaust valve. This is why you never use these white plastic PC seals. That carbon was created by oil that leaked past those seals. We will substitute a set of nice Viton rubber positive seals that will eliminate this nastiness. (Image/Jeff Smith)
We coated the lobes on our Summit Racing cam with the supplied moly lube and then carefully installed the cam followed by the timing set. We set the timing gears up with zero advance. (Image/Jeff Smith)
We generally find new cams install within 1 degree of accuracy and the Summit cam was equally accurate. The crank gear on the new timing set offers both 2 degree advance and retard slots that we could have used if necessary. Our cam measured 1 degree advanced but we’re going to leave it as it is. (Image/Jeff Smith)
With the new balancer installed, we decided to check the TDC balancer mark against the stock timing tab and discovered it was incorrect. The original 283 tab is pre-1969 style while the harmonic balancer places the keyway in the ‘69 and later position. This retards the TDC mark by 12 degrees. We fixed this by bolting on a 1969 and later timing tab. (Image/Jeff Smith)
Barrington rebuilt the heads with new Summit 1.72/1.50-inch valves, a good 3-angle valve job and quality valve guide seals. We set the heads up to ensure the springs were at the 1.770-inch installed height. (Image/Jeff Smith)
To improve the compression ratio, we used a set of Fel-Pro PN 1094, 0.015-inch compressed thickness head gaskets that move the heads closer to the pistons yet still give us 0.045-inch piston-to-head clearance while raising the compression to an excellent 9.43:1. (Image/Jeff Smith)
We set the preload on each lifter with the lobe on its base circle, finding zero lash, then setting the preload at 1/2-turn on the lifters. (Image/Jeff Smith)
Chevy changed the angle of the inner intake manifold bolts starting in 1987 for TBI engines. This is important because it’s easy to order the wrong part number intake manifold like we did. The traditional bolt pattern uses the same angle for all 12 bolt holes. The 1987-’95 TBI engines changed the angle of the inner four bolts, which requires a different intake manifold. The traditional pattern is on the left and the later ’87-’95 pattern is on the right. (Image/Jeff Smith)
To make sure the cam breaks in properly, we’re using Summit Racing’s Break-In oil that is fortified with higher levels of zinc and phosphorous (ZDDP) to establish the best initial wear pattern between the lifters and the cam. (Image/Jeff Smith)
Anytime we do major internal engine work, we always pressure lube the engine prior to starting the engine to ensure all internal components are coated with oil. We used an old distributor body and shaft as a pre-lube tool and made sure oil covered all16 rockers before completing the process. (Image/Jeff Smith)
We static-timed the HEI distributor at 12 degrees initial timing so that when we crank the engine it should start immediately. (Image/Jeff Smith)
We completed the engine with a mechanical fuel pump, short water pump and a pair of aluminum pulleys to complete the package. We bolted on a pair of stock ram’s horn exhaust manifolds that mount the alternator and with a new belt it’s now ready to run on our Summit Racing test stand. (Image/Jeff Smith)
We literally bolted the Summit Racing carburetor on the engine, prefilled the float bowl with the test stand’s electric fuel pump and the engine fired up almost immediately. Later, with a slight adjustment to the idle speed, the engine would idle with no other changes to the carburetor. Eventually we set the idle mixture slightly leaner but this carb was good right out of the box. (Image/Jeff Smith)

With our intrepid little small-block bolted to our run-in stand, it immediately started and ran. We brought the rpm up to 1,500-1,700 and ran the engine for three sessions of roughly 10 minutes each, allowing the engine to cool between. With the cam broken in, we’ll put about 50 to 100 miles on the engine and then drain the break-in oil and filter and be ready for the road! (Image/Jeff Smith)
We bolted on the Summit air cleaner just to check clearances to the distributor wires and our small-block is now complete and ready for the road. (Image/Jeff Smith)

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Author: Jeff Smith

Jeff Smith has had a passion for cars since he began working at his grandfather's gas station at the age 10. After graduating from Iowa State University with a journalism degree in 1978, he combined his two passions: cars and writing. Smith began writing for Car Craft magazine in 1979 and became editor in 1984. In 1987, he assumed the role of editor for Hot Rod magazine before returning to his first love of writing technical stories. Since 2003, Jeff has held various positions at Car Craft (including editor), has written books on small block Chevy performance, and even cultivated an impressive collection of 1965 and 1966 Chevelles. Now he serves as a regular contributor to OnAllCylinders.